Go to... | Start A New Topic | Search | Notify | Tools | Reply To This Topic |
8/11 |
Well, no sooner did I get one problem fixed (the generator), I ran into another. I have a MD3060 trans in our Barth and did a search on the forums and got some idea that my problem may be with the ECU? I am no mechanic and have no idea where to start, so here is my story: Went out yesterday to move the coach to it's winter storage. Started right up and everything is good. Went out to get a few things while the coach was warming up and returned to a burning smell inside the coach. Started doing a quick seek and search, but couldn't find the source. Went outside and found no smell of anything burning. Figured okay, it must be inside the coach. Came back in and still smelled the same but couldn't locate anything. Sat in the drivers seat and went to put the coach in reverse and noticed that the keypad was blank. Nothing showing on the keypad! Major concern as it had never done this before so I shut the coach down. Wait a minute or so and turn the key back on and I have nothing. No keypad, no red lights on dash, no ignition, nothing. I then notice a slight whisp of smoke coming from the keypad. Okay, I think I know where the burning smell is coming from. Pull the side cover off the console where the shifter keypad is located and the only thing I see is a box directly mounted under the keypad. The whisp of smoke has stopped already. So here is where I am right now: Is this box under the keypad my ECU? Any idea what might have happened? Any advice where to start to try to trouble shoot this problem? I cannot start the coach as it is right now so I can't take it to a repair shop. It's dead in our driveway. And after my last repair bill for the problem found (see my other post today), I'd like to try to see if I can find the problem and fix it myself with the help of those here. 9303 3855 33BS 1B Bruce & Kathleen 1993 33' Front Entrance Breakaway 230HP Cummins 5.9, Allison 6 speed, Spartan Chassis, Nicely Optioned | ||
|
03/22 |
Bruce, I am VERY concerned about this issue. If in fact the smoke came out of the shifter panel or the TCU, Not much you can do about this except replace the panel or TCU, BUT the main question is-----WHY----- This is the earlier model shifter panel and TCU, don't think they are available from Allison, and would have to be rebuilt. Will not be inexpensive. Anything else around the shifter panel or TCU that smoke could come from? Now that there is no power to start or power the instrument panel, some breaker or fuse has blown but look VERY CAREFULLY before replacing the fuse/breaker as further damage could be done. My shifter panel was replaced by the PO but I have no idea why or what the symptoms were. Go slow Ed 94 30' Breakaway #3864 30-BS-6B side entry New Cummins 5.9L, 375+ HP Allison 6 speed Spartan chassis K9DVC Tankless water heater | |||
|
2/10 |
Our control for the Allison went a couple of years ago. Came to start it in the fall---no lights in the pad and nothing happened when I turned on the key. There had been no issues prior to this-- it just happened( I didn't even get a smoke show!!) As Ed says, this is not an inexpensive thing to have happen. Replacement part has worked well since. Good Luck Bud 1993 Breakaway 36ft & 1977 20 ft Spartan: air ride and brakes & P32(?) Cummins: 8.3 litre 250hp, PACBrake Allison 3060 (6 spd) Front entry, side hallway 7.5 kw diesel gen. 1999 2dr Tracker 4X4 5spd, SMI Braking system | |||
|
9/09 |
I went through the same problem with my shifter (ECU). There is a discussion on that at My ECU Problem Lance & Sue Walton Previous owner of a 1993 38ft Regency Cummins 6CTA8.3 300HP Allison MD3060 Transmission Spartan Chassis Loveland, CO | |||
|
All I am currious about this... do you guys have a Stone Bennett shifter? I have a Stone Bennett and it sometimes sticks when I try to toggle to another gear. When I hit the toggle 2 or 3 times... it moves to the proper selection. I am hoping it is not a sign of a future failure and we get stuck somewhere. I believe mine is air activated. Jax 1990 32' Regency, Cummins 8.3 1990 32' Regency, Wide Body Spartan Chassis, 8.3 CTA Cummins 4 Speed Allison Trans South Central Missouri | ||||
|
3/12 |
Post pic of your shift pad and trans control unit.I may be able to help you out on the cheep! The first thing is to follow harness looking for chaffing ect. find your fues and relay and inspect. 15yr. working on them an never had the smoke escape from the shifter HaHa! Jax most issues with stone ar ground issues at the trans shift arm. also the contacts inside . Be CAREFUL part ar hard to find!! carl | |||
|
8/11 |
Well, I finally got to tearing my shifter apart to find the key pad smoked (literally per my previous post). The circuit board is black in one corner, obvious from where I saw the smoke rising from. Checked all the wiring going to the ECU and it all seems to be in tact with no damage. Sent both components away for testing and estimate to repair. They said it looks like something got down into the ECU at some time and then slowly started corroding it. And the smoking of the unit was the final outcome. Now, the bad and worse news... He tells me a remanufactured shifter panel and ECU is $3500 and if I want a "new" one, $4700. What? Hey, but the guy tells me that it includes programming it for the Barth, like that is supposed to make me feel good. So I ask how much is it to program the unit? He says $100! I tell him I just got to find my own replacement... H-E-L-P!!! 9303 3855 33BS 1B Bruce & Kathleen 1993 33' Front Entrance Breakaway 230HP Cummins 5.9, Allison 6 speed, Spartan Chassis, Nicely Optioned | |||
|
4/08 |
Check with Ted at www.tktsales.com. If it is allison related he is a great source. '92 Barth Breakaway - 30' 5.9 Cummins (6B) 300+ HP 2000 Allison Front entrance | |||
|
6/12 Formally known as "Humbojb" |
bud@YXY MWRENCH Steve VW Definitely need to check with bud's "replacement part" resource. Tere
| ||||||||||||
|
5/10 |
Maybe one from a wrecked one? Colaws in MO sells RV parts of all kinds and disassembles wrecked coaches Hope you and the coach get back on the road to recovery. 1999 Bluebird Custom 33' 8.3 Cummins diesel pusher Former owner 1989 Barth Regal 25' | |||
|
5/10 |
Http://Colawrvsalvage.com They got Allison ECUs (price?) 1999 Bluebird Custom 33' 8.3 Cummins diesel pusher Former owner 1989 Barth Regal 25' | |||
|
03/22 |
Hey Bruce, sorry to hear of all your troubles. Make sure you get and keep a record of all the numbers on the control unit and display unit. The MD3060 has gone thru transformations over the years and not all the electronics will be backward compatible. The display panel on mine was replaced by the PO and at that time it was $1200. I don't know why or what happened that triggered the replacement. Good luck in your search and have a speedy recovery! Ed 94 30' Breakaway #3864 30-BS-6B side entry New Cummins 5.9L, 375+ HP Allison 6 speed Spartan chassis K9DVC Tankless water heater | |||
|
8/11 |
Thank you Gary for the lead. Ted at TKT is the man! He will be hooking me up with a replacement controller and key pad later this week. Price for both, refurbished with 1 year warranty, is $1350. And that includes programming it for our Breakaway. 9303 3855 33BS 1B Bruce & Kathleen 1993 33' Front Entrance Breakaway 230HP Cummins 5.9, Allison 6 speed, Spartan Chassis, Nicely Optioned | |||
|
3/22 |
Bruce, Great News and a lot better $$$ money than expected Just curious how they program to your rig. What info did he need to do that? I am going to contact him to find out what/if/how I can do about getting DBarth to move when it is below 45 degrees! Dana & Lynn 1997 38ft Monarch front entry Spartan Mountain Master Chassis Cummins 8.3 325hp Allison MD-3060 6 speed 22.5 11R Cummins Factory Exhaust Brake 8000 watt Quiet Diesel Generator 9608-M0022-38MI-4C Christened Midnight 1972 22ft 72081169MC22C Christened Camp Barth | |||
|
3/22 |
If you have read some of the other posts on Allison MD-3060 6 speed. DBarth would not shift to any gear if it was below 45 degrees. Suggestions included RPM over threshold to shift because of temp. Tranny to cold. Emailed Ted and he suggested sending the key pad and ECU for replacement with rebuilt or evaluation by putting in the freezer. This got me thinking maybe as simple as warming these parts above 45 degrees. We got over a foot of snow that took down many trees and branches and made it like a mega snowball fight with someone trowing ice pail sized snowballs to get to DBarth this morning. 36 degrees and I wrapped a small 12 volt heating pad around the ECU and keypad. DBarth would not shift before applying heat. 10 minutes and it shifted to reverse and forward with little hesitation. So unbelievably simple. Heat the Key pad and ECU. I will make or modify a small 12 volt heater/tape or something. Such a simple easy thing having me pulling my hair out for 2 years. Saves me much $$$$$$ to be used for other projects. I know there were others with a similar issue here is the FIX!! Dana & Lynn 1997 38ft Monarch front entry Spartan Mountain Master Chassis Cummins 8.3 325hp Allison MD-3060 6 speed 22.5 11R Cummins Factory Exhaust Brake 8000 watt Quiet Diesel Generator 9608-M0022-38MI-4C Christened Midnight 1972 22ft 72081169MC22C Christened Camp Barth | |||
|
Powered by Social Strata | Page 1 2 |
Please Wait. Your request is being processed... |