Go to... | Start A New Topic | Search | Notify | Tools | Reply To This Topic |
I spent the whole day working on the 92 Breakaway 1st generator stopped cranking so I took out meter checked voltage and ohms 1st checked all connections nothing. I pulled the print board mounted on generator engine checked all capacitors and resistors cleaned board and plugged all ends in put back together still nothing. so I started checking all incoming plug connectors there it was a corroded pin to one of the in coming plugs replaced it started right up. Next replaced non locking lock on the propane door, then put a new water fill hose to water tank it had pin holes and started leaking. Good day in Barthland Now to write a new list of repairs. | |||
|
Official Barth Junkie |
It is good to have things working and you know they are OK. Low 40's and rain here. Looks like my Barth work will be on hold for a while. Florida sounds good about now. My coach is in getting new suspension parts, should be ready next week. 9708-M0037-37MM-01 "98" Monarch 37 Spartan MM, 6 spd Allison Cummins 8.3 325+ hp | |||
|
are you coming to Florida | ||||
|
Official Barth Junkie |
I plan to be at the Hillsborough GTG. Coach is in the shop getting new airbags and brakes, should be AOK for the trip. We are looking forward to meeting some more members. 9708-M0037-37MM-01 "98" Monarch 37 Spartan MM, 6 spd Allison Cummins 8.3 325+ hp | |||
|
Evan & Holly,Will you be in Palm Beach over Xmas and The New Year this year? 1993 34 Regency WB 8.3 Cummins 300HP | ||||
|
Yes anyone who wants to come stay with us are welcome | ||||
|
Steve call us I think you have my # if not let me know well be on West and east coast planning on lots of Barth miles this year | ||||
|
Powered by Social Strata |
Please Wait. Your request is being processed... |